Causes
The direct cause of the blowout was attributed to failure of subsea wellhead equipment after many hours of kick control. The Guardian reported that it was not known whether the blowout preventer (BOP) worked or if gas fractured the choke line at another point and burst through to cause the incident. Two survivors who were in charge of submersible video cameras that inspected the state of the equipment, including the BOP, told the Guardian that “the stand-by electric motor on the hydraulic system on the rig, which powers the BOP, was known to be burnt out, and that the annular preventer inside the BOP had been damaged and was not working for two days before the blowout.” ARCO responded that the Guardian reported factual inaccuracies, stating that the pressure rating on the blowout valve was adequate for the pressure. The Observer reported in 1990 that independent tests “uncovered allegedly dangerous welding faults in a high-pressure gas line on the rig.
After the rig was moved from location and the well bridged over, a remotely operated vehicle survey was conducted that discovered:
- BOP showed that the flexible choke line joining the rigid BOP choke line to the lower marine riser package (LMRP) had failed. Severe erosion was observed between the lower inner and outer choke valve actuators and the lower choke valve block. Fluid was venting from the valve block and the severed choke line.
- When the rig pulled off location, the LMRP failed to disconnect properly and the riser parted at the first weld on the first joint of riser. Drill pipe was draped over the top of the BOP stack and strung out to a distance of 35 feet from the BOP; the BOP was inclined at 1.4 degrees leaning to +315 degrees azimuth—the direction the rig pulled off location.
- The upper and middle pipe rams in the BOP were closed, the upper and lower failsafe kill valves were closed as was the lower annular preventer. Drillpipe and a bottomhole assembly had been hung off in the BOP.
Aftermath
In a Fatal Accident Inquiry, the Aberdeen's sheriff court criticized the Offshore Installation Manager and ARCO, stating:
“The death of Timothy Williams might reasonably have been prevented (i) if the Offshore Installation Manager (OIM) had not ordered him from the lifeboat to the radio room; (ii) if the OIM, having ordered Timothy Williams back to the radio room, had countermanded that order when the rig was evacuated, and taken steps to see that the countermanding order was communicated to him.”
ARCO representatives, the court concluded, had not followed safe and correct drilling practices including failure to correctly identify shut-in drillpipe pressure, failure to correctly calculate the circulation time of the gas kick, and failure to shut in the well once the well began flowing uncontrollably.
For some years after this incident, the UK Department of Energy banned drilling in areas with anticipated reservoir pressures in excess of 10,000 psi.
The Ocean Odyssey spent several years rusting in Dundee's docks. But it has since been redeveloped as an ocean-going satellite launch pad called Sea Launch. It is based at Long Beach, California where the spacecraft are assembled before the rig is relocated to the equatorial Pacific Ocean for launch.
Practical Lessons
- Stop work if you consider it unsafe
- Assess and understand major hazards and potential accident events
Ensure that this assessment addresses possible impact on escape, temporary refuge, and evacuation facilities. The assessment also should provide input into the facility philosophy for escape, temporary refuge, and evacuation along with emergency response requirements.
- Test emergency response capability against potential major accident events
A better understanding of the hazard and potential accident event consequences along with testing and familiarity with the response requirements and equipment might have resulted in the radio room operator not being sent back to the radio room.
- Once the decision is made to board the lifeboats and evacuate, it should include all personnel
No one should still be trying to control the incident. Lifeboats then can be launched as soon as boarding is completed.
Furthermore, the 2005 UK Health and Safety Executive (UK HSE) report on high pressure, high temperature developments lists industry practices to prevent future events including:
- Intensive quality assurance procedures
- Design changes to well configuration
- New inspection processes
- Special handling and installation procedures
- Selection of experienced design and operating teams
- Use of supply and service resources with a proven track record
- Open exchange of information between HPHT operators
References
Beavis S. (n.d.) Report alert ‘could have saved oilmen.’ (publication unknown).
Bowcott O, Hetherington P. (n.d.) Fluid leaks ignored on blow-out rig. Guardian.
Ocean Odyssey (modified 6 March 2009). Wikipedia. Online at http://en.wikipedia.org/wiki/Ocean_Odyssey . Accessed 19 August 2009.
Gillespie JD, ARCO Alaska Inc.; Wann KE, ARCO British Ltd. (1990). The Ocean Odyssey: Well Control Project II. IADC/SPE Drilling Conference, Houston, Texas. Abstract Online at http://www.onepetro.org/mslib/servlet/onepetropreview?id=00019916&soc=SPE . Accessed 19 August 2009.
High pressure, high temperature developments in the United Kingdom Continental Shelf. Research Report 409 (2005). Highoose Limited for the U.K. Health and Safety Executive. Online at http://www.hse.gov.uk/research/rrpdf/rr409.pdf . Accessed 19 August 2009.
Radio order caused rig death, says union. (28 November 1989) Guardian News and Media Limited.
(3576) Report to EERTAG on Ocean Odyssey Survivors Report (1997). United Kingdom Health & Safety Executive. Online at http://www.hseresearchprojects.com/projectsearch.aspx?id=1055 . Accessed 19 August 2009.
Photo References
File:OceanOdyssey.jpg. Wikipedia. Online at http://en.wikipedia.org/wiki/File:OceanOdyssey.jpg Accessed 25 September 2009.
Ocean Odyssey (n.d.). Versatel. Online at http://home.versatel.nl/the_sims/rig/o-odyssey.htm . Accessed 19 August 2009.
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